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Rainway inspector
This is the first project we cooperated with HKPC and MTR for the railway track inspector robotic machine.
The project aim was to create the 4G automatic check for railway checking daily usage.
From the concept idea stage to working prototype execution, the ARV team totally spent 6 months on the project.


The biggest challenge for the project was the cart and how to self-balancing on the track but at a low cost.
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